NCP1031: Dual output, 4 W DC-DC converter

DN06046/D
Design Note – DN06046/D
Dual Output, 4W DC-DC Converter
Device
Application
Input Voltage
Output Power
Topology
I/O Isolation
NCP1031
Vacuum Fluorescent
Display power
supply
26 Vdc
4W
Flyback
Yes
Output Voltage
Nominal Current
PFC (Yes/No)
Inrush Limiting / Fuse
Operating Temp. Range
Cooling Method /
Supply Orientation
Signal Level Control
Output 1
Output 2
5V
200 mA
14 V
200 mA
No
NA
0 to +50˚C
Convection
No
Others
Circuit Description
This Design Note illustrates a dual output, 4 watt, isolated
dc-to-dc converter originally intended for fluorescent
lighting applications. The converter is designed around ON
Semiconductor’s NCP1031 monolithic dc-to-dc switcher
IC. The chip contains all of the control functions for a low
power converter including an integrated 200 volt internal
Mosfet. This particular design, with the appropriate circuit
and component modifications can also be made to operate
with nominal dc input voltages anywhere from 12 volts to
70 Vdc and with other output voltages depending on the
particular application.
The dc input includes an EMI/ripple filter comprised of L1
and C1 followed by a flyback dc-to-dc converter composed
of transformer T1, and U1, the NCP1031 controller/Mosfet.
Once started via the input voltage on pin 8, the controller
operates from an auxiliary Vcc voltage generated by the
lower primary side bias winding of T1. This voltage is
rectified by D2 and filtered by Vcc capacitor C5.
The NCP1031 includes input over-voltage and undervoltage shutdown sensing via pins 5 and 6 respectively. To
minimized voltage spikes created by T1’s leakage
inductance, the snubber network of D1, C3 and R1 is
included. Output overload protection is also provided
within the NCP1031 by sensing the peak Mosfet current.
September 2008, Rev. 0
Output regulation is accomplished by sensing the 5 volt
output, dividing the sense voltage to 2.5 volts with R9 and
R10, and utilizing a TL431 programmable zener as an
error amplifier to drive a feedback signal to U1 via
optocoupler U2. Loop phase compensation is provided by
R11 and C13. A ripple filter is provided by L2 and C10 to
reduce the 5 volt output ripple and noise to a very low
level.
The 14 volt output is developed by “stacking” an additional
number of transformer secondary turns on top of the 5 volt
output. This stacked winding technique provides enhanced
regulation of the “quasi-regulated” 14 volt output due to the
fact that the initial 5 volts of this output is the fully
regulated 5 volt output. A small pre-load (R6) is provided
to avoid upward voltage creep if the 14 volt output is
unloaded.
Key Features
y Input EMI/ripple filter
y Simple, inexpensive flyback topology using monolithic
dc-dc switching IC
y Dual regulated outputs
y Input UV and OV protection in addition to output short
circuit protection
y Can be easily tailored for other input – output voltage
configurations by changing transformer turns ratio and
appropriate component ratings
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DN06046/D
Schematic
L1
4.7uH
T1
D3
8
26Vdc
Input
C1
C2
0.1uF
50V
R1
10K,
0.5W
C3
2.2nf,
250V
220
50V
D1
1N4002
R2
47
R4
3.9K
8
4
U1
7
ov
2
5
1 3
C4
1nF
C8
0.1
R6
2K
L2
4.7uH
MBRA140
+ 5V
3 D4
1N4148
2
7
6
R5
3.9K
C7
470uF
25V
D2
NCP1031
uv
+14V
MBRA140
5
1
R3
47K
4
6
C9
1000uF
6.3V
C10
100uf
10V
C11
0.1
Com
R7
180
C5
10uF
U2
R8
1K
C6
4.7nF
C12
4.7nF
"Y"
NOTES
C13
R9
2.2K
0.1
1. R7, R8, & R9 sets converter input UVL and OVP points.
2. U2 is Vishay SFH615A-4 or equivalent.
3. L1 and L2 are Coilcraft LPS3008 or similar (4.7uH, 500mA).
4. T1 is custom flyback xfmr on EF-16 core (see design sheet).
5. Crossed lines on schematic are not connected.
U3
TL431
R11
3.3K
R10
2.2K
Dual Output, 4 Watt DC-DC Converter using ON Semi NCP1031
Additional collateral from ON Semiconductor
y NCP1031: Current Mode Controller Fixed Frequency Operation
y MMSD4148 (1N4148): 100 V Switching Diode
y TL431A: Programmable Precision Reference
y MBR20100: 1A, 40 V Schottky Rectifier
y Application Note AND8247: 5.0 W to 6.5 W Power Over Ethernet (PoE) DC-DC Converter
y Application Note AND8119: Design of an Isolated 2 W Bias Supply for Telecom Systems Using the NCP1030
y Design Note DN06007/D: Wide Input Range (20 Vdc to 140 Vdc) DC to DC Converter
September 2008, Rev. 0
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DN06046/D
1
Magnetics Design
NCP1031 Flyback Xfmr Design
Part Description: 5 watt, 200 kHz DCM flyback transformer, 5/14 volts out, 26 Vin
Schematic ID: T1
Core Type: Ferroxcube EF16 (E16/8/5); 3C95 material or similar
Core Gap: Gap for 60 - 70 uH
Inductance: 65 uH nominal
Bobbin Type: 8 pin horizontal mount for EF16
Windings (in order):
Winding # / type
Turns / Material / Gauge / Insulation Data
Vcc/Boost (2 - 7)
9 turns of #28HN spiral wound over 1 layer. Insulate
with 1 layer of tape (250V insulation to next winding)
Primary (1 - 8)
24 turns of #28HN over 1 layer. Insulate for 500V
minimum to the next winding.
5V Secondary (3 - 6)
5 turns of 2 strands of #28HN flat and spiral wound
bifilar evenly over 1 layer; self leads to pins.
Insulate with tape.
14V Secondary (4 - 5)
9 turns of 1 strand of #28HN spiral wound over
1 layer. Self leads to pins. Insulate with tape.
Hipot: 500V from Vcc boost/primary to secondaries
Lead Breakout / Pinout
Schematic
(Bottom View - facing pins)
8
4
Pri
14V stacked sec
5
1
2
Vcc
3
5V sec
4
3
2
1
5
6
7
8
6
7
1
© 2008 ON Semiconductor.
Disclaimer: ON Semiconductor is providing this design note “AS IS” and does not assume any liability arising from its use; nor
does ON Semiconductor convey any license to its or any third party’s intellectual property rights. This document is provided only to
assist customers in evaluation of the referenced circuit implementation and the recipient assumes all liability and risk associated
with its use, including, but not limited to, compliance with all regulatory standards. ON Semiconductor may change any of its
products at any time, without notice.
Design note created by Frank Cathell, e-mail: [email protected]
September 2008, Rev. 0
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